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T. H. Huffman
Interoffice Communication
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Subject:
d. C. Skokna January 17, 1989
ABERDEEN MONTHLY PROGRESS REPORT - DECEMBER, 1988
Safety
There was one first aid and one recordable case reported during December. As of December 31, the plant's employees had worked 3467 days or 4,539,724 manhours since the last lost time injury.
Kev Statistical Information
PVC Production, MM Lbs. Reactor Stream Factor, % Resin Quality, % Prime VCM Efficiency, Lbs./Lb. Flexible Compound Production, MM Lbs. Flexible Compound Quality, % Prime Rigid Compound Production, MM Lbs. Rigid Compound Quality, % Prime Plasticizer Production, MM Lbs. Plasticizer Quality, % Prime Energy Use, (EUI %) Fixed Cost Variance, $M Variable Cost Variance, $M Variable Cost Price Variance, $M Variable Cost Efficiency Variance, $M
Costs
December
38.7 92.1 95.8 1.0182
6.6 96.7
5.6 99.9
1.7 97.7 (4.5) (57.4) 520.2 400.1 120.1
Y.T.D.
115.2 91.7 95.7
1.0165 19.0 94.2 16.8 99.9 5.3 94.5
(2.6) (136.2)
1420.8 1393.0
27.8
Fixed costs in December were above budget due to payroll, which was high due to holiday pay and staffing salaried positions sooner than was budgeted; MM&C, which was caused by early completion of some budgeted projects as well as completion of several unbudgeted projects; and moving/home assistance clearances. These were offset somewhat by lower than budgeted outside professional service charges.
Variable efficiency costs were favorable due primarily to good operation of the dry blend unit.
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VAB.0001190635
DISTRIBUTION
COVER LETTER
ENTIRE REPORT
Houston
J. D. Burns
X
R. T. Ferrell
X
T. H. Huffman
X
C. J. Matson
X
D. F. Harman
H. R. Flammer
X X
R. R. Smith
X
K. J. Eggers
X
R. H. Gerlach
X
Ponca Citv
S. E. McGuire
X
R. L. Poe
X
H. J. Hall
X
Oklahoma Citv
H. G. Garrison
X
LCVCM Plant
R. A. Conrad
X
LCCP Plant
J. Friend
X
LCLAB Plant
J. W. Ware
X
Baltimore
L. R. Bauer
X
Hammond
J. B. Maher
X
Blane
C. R. Miller
X
Premiere
P. L. Foote
X
Aberdeen
RWS/DCS (File Copy), PJK, JEN, DWH, TFL, JEB, HGC, JEL, REP, BLT, RBN, SCH
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VAB.0001190636
T. H. Huffman 1/17/89 Aberdeen Monthly
Page 2
s Report - December, 1988
QMS
Fifteen people group will goals.
trained to be facilitators. This our teams in progressing on thei
hosted a meeting of the Manufacturing The Aberdeen Plant Site Coordinators.
involved in the 5305 Resin Several plant people were Quality Improvement Team.
D. C. Skokna Plant Superintendent
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SAFETY - B. L. Trego, J. V. Uptain December
Fiscal Y.T.D. 1989
Fiscal Y.T.D. 1988
First Aid OSHA Recordable
Total Injuries
Number of Restricted Workday Cases Number of Lost Workday Cases
0 1 1
1 0
Injuries bv Department
Vinyl Operations Compound Operations Maintenance Laboratory Receiving/Warehouse Office
Totals
Injuries bv Type
Cuts and Abrasions Eye Injuries Burns Bruises Strains/Sprains Stings Other
Totals
0 1 1 0 0 0 2
0 0 0 1 0 0 1 2
Non-Occupational Injuries
Lost Workday Cases Days Lost
0 6
Safety Record
Last lost time injury - 7/5/79
Days since -
3467
Manhours since -
4,539,724
On December 31, 1988, the employees of the Aberdeen Plant completed 3467 days with no lost time injury.
Topics for the plant safety meetings during the month included: Winter Operation, Safe Use of Torque Wrenches, Yearly Review of Injuries, Planning for Safety, Hydroblasting Safety, and Maintenance Weekly Safety and Job Review.
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SAFETY - continued
Chemical
< PEL Number Percent
> PEL________
Number
Percent
VCM Lead Total Particulates
73 100.0 16 100.0
3 100.0
0 0 0
0.0 0.0 0.0
Monthly Inlurv Summary
Iniurv Class
Department
Description
Compound
Muscle strain, right upper back and shoulder.
RWC
Maintenance
Fracture, 5th right finger.
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(Twelve Month Running Totals)
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TOTAL INJURIES
0 OSHA RECORDABLE
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QUALITY DEVELOPMENT - D. W. Hollis
General Plant
Facilitator training was given to fifteen people. provided for all teams to help the team leader.
Facilitators will be
The Aberdeen Plant hosted a meeting for the Manufacturing Site Coordinators to share ideas on past and future QMP methods.
The Plant Manager's Natural Team met once during the month to continue working on removing barriers to QMP implementation.
Administrative Services
Jack Little met in Houston on December 6, 7, and 8, to participate in the "OASIS" software demonstrations. American Software, Inc. and Cullinet Software, Inc. were scheduled to demonstrate test scripts by various members of the "OASIS" team.
Mike Swierc met with the CQIP team in Lake Charles on December 8.
Pat Wells attended the facilitator training session.
Compound
The Compound Superintendent's Natural Team met in December. The meeting included a review of last year's performance and departmental goals for this upcoming year.
Each shift supervisor's natural team met in December. The "B" shift supervisor's natural team traced out and identified product transfer lines.
Lab
SQC techniques were used to examine the 1988 RP-421 WHT 110 data on shipments to Vycom. The data was used to exhibit product consistency in a customer call.
Four of the six lab's natural teams met in December.
Mechanical
The Mechanical Superintendent's Natural Team met once during the month. The topic was Project Team Updates and Team Facilitation.
The Engineering Team process flow chart was revised and will be issued for review in February.
Process Engineering
The Department Heads' Natural Team met in December to discuss recruiting and department training needs.
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QUALITY DEVELOPMENT - Continued
Process Engineering - continued
Two days of in-depth PVC training was conducted by R&D for the plant.
Several process engineers were involved in a one-day facilitator training class.
Vinvl
The department's natural team met twice during the month to coordinate daily operations, discuss Klockner quality issues and action steps, review employee action team progress, and to continue work on the Quality Implementation Plan.
The Railcar Cleaning Team has completed their activity and construction will soon begin on the cleaning system. The 5265/5305 Contamination Team's activities have been taken over by the "full time" Klockner Contamination Team. The Alcohol/Plasticizer Team has completed the alcohol unloading portion of their problem and have begun work on the plasticizer portion. The V-ll Dustbusters are continuing with their work on modifying one of the Sweco/activator systems in the rotary dryer area.
P. J. Kober attended a meeting with Klockner personnel on contamination. A presentation was made to Klockner regarding the work Vista has done and will be doing in short and long term to improve in this area. The presentation included personnel from Manufacturing, R&D, Business Area and Marketing. The presentation was well received by Klockner.
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COST VARIANCES - D. C. Skokna
Variable Costs
Product
December 1988 Variance. $M
Efficiency
Price
Total
PVC Flexible Compound Rigid Compound Plasticizer
$32.6
20.6
83.3 ( 16.5)
$120.1
$354.5 ( 3.2) ( 17.9)
66,7 $400.1
$387.1 17.4 65.4 50.2
$520.2
PVC - Efficiencies were essentially at budget.
Flexible Compound - The variance was primarily due to product mix.
Rigid Compound - The favorable variance was primarily due to product mix and good Ti02 efficiencies.
Plasticizer - The variance was primarily due to low VRP production.
Price Variances
Item
$M
VCM
$393.0
Alfol 610
55.1
610P
34.4
Colorants
19.0
VCM Freight
17.7
Natural Gas
(42.2)
All Other Price Variances
(76.9)
Total $400.1
Fixed Cost Variances
m
Payroll and Benefits MM&C Miscellaneous TI&D Clearances
Total
($29.6) ( 47.8)
10.5 2.9 6.6
($57.4)
Payroll and Benefits - was above budget as anticipated below par salaried staffing did not happen. Salaried staffing has been above budgeted level (budget -- 75, actual -- 78). Also, overtime was high due to the Christmas holiday.
MM&C - Some maintenance projects were completed ahead of budget.
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COST VARIANCES - Continued
Miscellaneous
Outside professional services were $23.5M favorable as PL&D work for the DCS project and the air modelling study did not begin as budgeted.
Contract-operating was $14.8M favorable due to not needing an operating contract for the Coker water test run.
Shipping costs were $12.3M unfavorable due to late processing of an invoice. This rail switching invoice should have cleared in November.
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OPERATIONS AND MECHANICAL DEPARTMENTS - P. J. Kober, Ted Lyon, Ted Nickerson
Operations/Mechanical Safety
There was one recordable injury resulting in restricted duty in the Mechanical Department in December. A General Mechanic suffered a lacerated and fractured finger while working on the #6 dryer centrifuge. The injury resulted when a belt guard was inadvertently dropped during maintenance work. There was one first aid injury in the Compound Department during the month which involved a pulled muscle suffered by a Plasticizer Operator. The Vinyl and Yard Departments worked without injury in December.
Monthly safety meeting topics included: winter operations and hazards, hydroblasting and hydraulic torque wrench operation and hazardous wastes.
The Compound Department experienced one first aid case in December. (Final classification of this injury has not been determined at this time.) An employee strained his back while operating a large valve.
The December monthly safety meeting covered concerns associated with hazardous wastes and included RCRA training.
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VINYL - P. J. Kober, C. J. McDonald
General
1. 5305 was made in reactor D744 for a week. The reactor walls
remained clean. Reactor dump slurry contamination was lower
than reactors D700 and D745.
Three and three-fourths
railcars were produced.
2. Additional test of Coker water as charge water was performed this month. The conclusion is still that no buffer is needed. This concluded testing of the Coker water.
3. Dryers #4 and #6 were hydroblasted as part of 5305 contamination reduction testing. We now clean the dryers every other day as standard procedure for low molecular weight production.
4. The resin raw materials in the 744 account were valued at $433.1M.
December
YTD
- Production - Daily Rate, M Lbs./C.D. - Total Reactor Charges - Charges/C.D. - Reactor Stream Factor, % - Rotary Dryer Stream Factor(#4-#8), - Fluid Bed Dryer Stream Factor, % - Resin Quality, % Prime
%
Reactor Downtime
38.7 1249 924
29.8 92.1 83.1 97.5 95.8
115.2 1253
2735 29.7 91.7 85.4 96.5 95.7
Hours
Operational downtime (recovery scheduling conflicts, power failure, downtime to rinse chem wash tanks, New Module rinse/charge water conflicts, waiting on particle size data before charging, precharge and dump preparations for Coker water test batches, false charging 5305 ingredients for D744 5305 test, and manual preparations for D744 5305 dumps).
348.7
Maintenance downtime (hydroblast D745 reactor shell and condenser, hydroblast D744 reactor shell and condenser, no place to dump while fluid bed dryer screw feeder was repaired, AMS emergency kill system repairs, change VCM receiver inert vent line, chem wash tank level indicator repair, new unit F50 meter repair, change relief valves on D744 for 5305 test, install line from D744 to low molecular weight dump line, and miscellaneous instruments & valves.)
237.5
VINYL - continued
Reactor Downtime - continued
Total downtime was 586.2 hours.
Drver Downtime
% of Total Downtime
Reactor limited production
79.7
Operational downtime (centrifuge plugging dryer cleaning, activator transfer problems, checking dust collector socks for leaks, flameouts, checking sifter screens, dust collector back-ups, and power failure.)
8.3
Maintenance downtime (fluid bed screw feeder, hydroblast #4 and #6 dryers, fluid bed screener repairs, Star valve repairs on #6 and #8 dryers, install permanent calcium stearate feeder on #5 dryer, low molecular weight slurry feed pump, and various activator and centrifuge repairs.)
12.0
Key Maintenance Work - D. A. Miller, J. B. Hegwood
Reactor Area
Reactor 744 was shut down for hydroblasting. The condenser
which is normally drilled was also hydrobias ted.
The
hydroblasting of the condenser was done in order to evaluate
the possibility of hydroblasting instead of drilling the
condenser. It was determined that the reactor condeners
could be hydrdoblasted effectively. This will reduce the
amount of time required to do this job significantly.
The old reactor unit rinse water pump was shut down for repairs due to a leaking seal. The shaft and bearings were replaced and the pump was put back in service.
The old reactor unit's "B" recovery compressor was shut down for repairs on its shaft. The shaft was pulled, repaired and re-installed.
The old reactor unit's "A" vacuum pump was changed out due to a leak in the case caused from excessive erosion.
The new reactor unit's 901 vacuum pump was replaced due to a leaking case.
New controls were installed in the vinyl unit control room for the new chem wash control system. The existing pneumatic temperature control system was replaced with a new electronic temperature control system.
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VINYL - Continued
Kev Maintenance Work - continued
The chem wash backflush system was modified in order to optimize its performance.
The Gould Modicon program was modified to prevent the reactor atmospheric vent valve from opening above 4 psig. This was done in compliance with an Employee Safety Action Request.
There were ten major valves changed out in the reactor area during the month.
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COMPOUND
General
All compound lines (including the dry blend unit and plasticizer) were down December 24-26 for the Christmas holiday.
The first extended production of 38401 Orange compound took place
on Line V. This production run extended over ten days and yielded
approximately 400M pounds.
Compound color was maintained
consistently on target throughout the run.
Operating
Compound Production
Davs
Production fM Lbs.l Month Avg./Dav Fiscal Y.T.D.
Line I Line III Line V
Total
28 28 23
2092 3578
882 6552
75 128
38
6124 10422
2496 19042
Downtime
Hours
Line I
- Product Changes - Transfer Problems & Limitations - Quality Problems & Control - Dicer Problems - Miscellaneous Maintenance
Line III
- Product Changes - Quality Problems & Control - Transfer Problems & Limitations - Mill Joint Repair - Miscellaneous Maintenance
59 12 10 10
8
Line V
- W&P Maintenance - Product Changes - Orbitran Panel Maintenance - Miscellaneous Maintenance
41 32 20
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COMPOUND - Continued
Operating Days
Month
Production (M Lbs.) Fiscal Y.T.D.
Rigid Compound
28
5586
200
16790
Downtime
Hours
- Product Changes - Quality Problems & Control - Univox Problems - Miscellaneous Maintenance - Welex Problems
41 19 18 15 14
Operating Davs
Month
Production (M Lbs . )
Avg./Dav
Fiscal Y.T.D.
1655
5340
Kev Maintenance Work - D. A. Miller, J. B. Hegwood
- Several tubes that were leaking in the tank farm Glycol unit condenser were plugged to prevent further leaking. Also, the condensate line for the condenser was re-routed in order to separate the high pressure condensate system from the low pressure condensate system. This revision prevents the high pressure condensate system from leaking back into the Glycol heat exchanger.
- A plate was installed around the charge station on Line III as part of a project initiated by the Lead Abatement Team.
- After repeated seal failures on the phthalic anhydride transfer pump, a new bellows-type mechanical seal and steam jacketed gland were installed. To date, the new seal has performed well.
- The Line V compounder was shut down by a failure of its DC drive control board. The DC drive control board was replaced and the Line V compounder was put back in service.
- The blades in #1 Welex were changed due to normal wear.
Utilities
- The API separator was bypassed and drained in order to clean out as much of the settled particulates as possible.
Number two boiler was painted and run on low fire
periodically during the month. It was
put back on
line during the month and #1 boiler was put on standby.
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COMPOUND - Continued
Utilities - continued
- After completion of the piping upgrades to the west propane storage tank and all of the mixed gas storage tanks, the plant was run on propane for approximately three hours in order to check the integrity of the upgrades.
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ENGINEERING - R. E. Polk, S. C. Hillman, V. L. Thornhill
Projects In Development - General
The Klockner Contamination Team completed Its investigation of
contamination sources. A meeting involving the plant, Business
Area, PED and R&D was held to establish goals for reducing
contamination.
Team findings and plans for improvement were
presented to Klockner on December 20.
5305 In 744 Test Run
Test production of 5305 resin in 744 reactor was successfully completed and a report Issued. The test showed that 5305 made in small reactors will meet our 5305 specifications. Customer trial of the resin still needs to be done.
Lead Handling and Exposure Reduction
A program has begun to reduce the amount of lead the color weigh room operator handles by rounding compound batch sizes to even bag weights of lead where possible. Thus far, twenty-six formulas have been rounded off to reduce color weigh room lead handling.
Coker Water Test Run
Two additional runs were tested in reactors 741 and 742 to evaluate the effects of chem wash on the sodium levels on the resin. Testing is complete and the test system will be dismantled and returned. A water balance is being prepared for designing the new Coker water supply system.
Vinvl DCS
A meeting was held with GED and plant personnel to review the timeline for engineering tasks needed to determine system costs.
Chlorine Gas Monitoring System
A design to install a chlorine gas monitoring system at the chlorine ton cylinder storage area was issued for plant review.
Recruiting
By the end of December, nineteen process engineering and thirteen mechanical engineering plant interviews had been completed. There has been one process engineering job acceptance and two mechanical engineering acceptances. All are scheduled to start work in midJ anuary.
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THE Sft MODULE IS OPERATIONAL IWTH PUNCHLISTITEMS IN PR06RESS.
DELIVERY OF THE REMAINING ITEMS ARE EXPECTED INJANUARY. CLOSED TO FIELD CHARGES IN JANUARY. CLOSED TO FIELD CHAR6ES IN JANUARY.
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RESIN QUALITY IMPROVEMENTPROJECTS
CRITICAL SPARE EQUIPMENT
PROPANE TANK FARM REMOTEOPERATED VALVES PA FLUF CONTAINMENT
F786/F557
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Water
All wastewater discharge parameters were within NPDES limits for the month of December.
Air
The annual VCM flange and valve survey was completed. A list of all the leaks found and their locations was issued. Seventy-one leaks were found.
A bagging study was completed by Emissions Control Services. Twenty-one of the leaks found in the annual survey were bagged. An additional sixteen components (flanges, valves, etc.) were bagged as non-leakers or zeros. All of the data from these bagged components will be used to develop fugitive emission factors for the components in our plant. These fugitive emissions factors will then be used to calculate the total fugitive emissions for the plant. We are required to report fugitive emissions annually under SARA Section 313.
A bleeder valve survey was conducted in the New Module area. Two bleeders were found to be without the required plugs. About one-third of the bleeder valves were repainted.
Waste Management
December waste shipments included:
- Two bulk tanker loads of separator oil to Stauffer Chemical
- One dump truckload of floor sweepings to Chem Waste Management
- One truckload of reactor culls in super sacks to Sun Polymers
In addition to these shipments, the API separator was bypassed and the solids/sludge was cleaned out of this pit. One roll-off container (20 cubic yards) was filled with the solids/sludge and shipped to Chem Waste Management.
Gaylord box samples of pond #2 resin, stormwater pit #1 solids and stormwater pit #2 solids were sent to Sun Polymers and KREO Company in an effort to sell this material. We currently have about 20MM pounds of pond #2 resin and about 175M pounds in each of the stormwater pits.
Annual RCRA training was completed for all four compound shifts.
In calendar year 1988, 867M pounds of hazardous waste was disposed of at a cost of $52M.
Miscellaneous
Coordinated and attended In-Depth PVC Training course held at the plant.
A
VAB.0001190654
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ENVIRONMENTAL - continued
Updated and re-issued the Spill Prevention Control and Countermeasure (SPCC) Plan. Also, completed semi-annual inspection of dikes and trenches around potential oil spill areas which is required by the SPCC Plan.
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ENERGY CONSERVATION - D. A. Moore
December 1988
Fiscal Y.T.D.
I. Energy Conservation Data
A. Unadjusted EUI B. Adjusted EUI C. BTU/Lb. Product D. Total Energy Consumption MMM BTU
-4.52% -4.18% 2543.96 133.48
-2.63% -2.23% 2496.13 389.94
This corresponds to anadjusted CMA of and an unadjusted CMA of
51.25% 39.44%
51.92% 40.56%
II. Plant Energy Conservation Program
A. Maintenance
There were ten energy related items completed in December, 1988. Nine of these items were steam leak repairs. The remaining one was a steam trap repair.
Ill. Boiler Operation
Boiler
Combustion Efficiency % Dec..88 Fiscal Y.T
No. 1 No. 2 No. 3
83.44%
(1) 83.20%
83.55% 83.57% 83.20%
(1) Boiler #2 was not operated during the month *
A
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VAB.0001190657
HUMAN RESOURCE REPORT
PERSONNEL - J. E. Beall
EMPLOYMENT None
PROMOTIONS/TRANSFERS Dale Barr promoted from Compound Operator to Compounder. Ricky Clay promoted from General Helper to Compound Utility. Maurice Evans promoted from Compound Utility to Compound Operator Phil Hall promoted from Compound Utility to Compound Operator.
RETIREMENTS None
TERMINATIONS/RESIGNATIONS Brian Aftergut Todd Haley Lee Lusk
TO/FROM LEAVE OF ABSENCE None
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Aberdeen, Mississippi
Salaried Employees Hourly Employees Total Employees
Employees (Hourly) New employees Terminations
DEPARTMENTS Warehouse
en. Plant Maintenance Laboratory Compound Vinyl Plasticizer
PAR 16 13 41 24 40 33
5
78* 169 ZA1
DECEMBER, 1988 MONTHLY PERSONNEL REPORT
Minority Employees
Salaried Hourly
7
66
Total
%
21 39% 2Q1
0
Hourly Min. Hired
0
0 % Min. Hired ___Q_____
Hourly Min. Term.
0 - ..
% Min. Term.
0
# EMPLOYEES MIN. EMP. % MIN. NEW HIRES YTD TERM. YTD TURNOVER
16 7 12 7 39 10 24 4 40 26 33 10
52
44 __
0
0 00
58
0
10 0
00
25 _Q
00
00
17 _ _ Q
00
00
65
_ 0___
00
00
>i
30 0
00
00
40 0
00
00
Number of Applicants
Month
0 Year to Date
APPLICANT BREAKDOWN:
// Minority 0
% Minority
# Female
0
% Female
35
0 0
* Includes 2 Co-op Engineers
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Month
Q Year to Date 10
Terminations (Hourly):
Month
l
Year to Date 6
Overall Turnover
.6%
Projected Annual Turnover
3.6%
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ADMINISTRATIVE SERVICES - J. E. Little
There were no safety instances this month. Safety meetings stressed offthe-job injuries and extra caution during holidays.
Cost Savings
Savings due to competitive bidding were $8995 for the month, and $20,859 for FY1989.
Savings due to prompt payment discounts were $1912 for the month, and $5974 for FY1989.
The switchover to the new AT&T switch was completed December 29, 1988. Thanks to Judy, and pre-planning by AT&T, this was a smooth transition. Judy Frossard and Jack Little will attend an AT&T sponsored class on the new System 75 January 16-20, 1989.
Internal Audit
Vista's internal auditors arrived December 5, 1988, to conduct their scheduled operations audit - two weeks. An exit interview was held with them on December 16, 1988. The auditors should have a draft of their audit exceptions prepared by late January. We will review and comment before the final report is issued.
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SHIPMENTS BY PRODUCT - M LBS. RESIN PLASTICIZER DRYBLEND COMPOUND
NUMBER OF SHIPMENTS BY MODE:
TOTAL
Dec. 1988
27,272 631
4,213 6,552
38,668
RESIN-Bulk
FISCAL YEAR-TO-DATE
82,543 2,135
13,423 21,634
119,735
A
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TOTAL DEC. OCT. NOV.
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LABORATORY - H. G. Coleman
A. Safety - The Lab operated Injury-free this month. There were no Incidents the entire calendar year. The monthly
meeting, presented by H. G. Coleman, included a review of the FY89 Safety Statistics for the plant and a "Safety Seconds" film entitled Pre-Flight Your Job.
B. Customer Relations
Customer Contacts
12/1 -
Brian Harrison visited Vinylex in
Knoxville, TN, along with M. C. Manion, M.
Washington, and C. 0. Yoder.
Topics
discussed included color and dry blend Q.C.
12/8 -
Brian Harrison accompanied Tom Davis to Vycom to discuss product consistency of RP-421 and Aberdeen's production and Q.C. operations.
12/9 -
Brian and Tom visited United Thermal Plastics to discuss several processing problems this dry blend customer was having.
Requests for Corrective Action
Date
Customer
Product
Reason
12/5
Master Halco
45541 Natural Stringers, zippers
Customer Problem Reports
There were no customer problem reports received this month!
Waivers Issued
Customer
Product
Reason
No.
Essex
5415
Bulk density
1 R/C
Hayes Dockside
80273G
40 mesh
1 R/C
Southwire
5415
Bulk density
1 R/C
RVCM Summary
RVCM of In-Process Samples
The following is a summary of residual VCM results on inprocess samples. None of the reactor daily average 400 ppm RVCM during the month of December, 1988.
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LABORATORY - continued
C. RVCM Summary - continued
Reactor Slurries
Drier
5265
5305
Number of Samples Average RVCM, ppm
923 133
25 0.400
96 0.315
RVCM of Shipment Samples
The following is a summary of the residual VCM analysis of shipment samples for the month of December, 1988.
Product
Number of SamDles
Average RVCM. ppm
5265 5305 5385 5415 5465 Dry Blend Debox Pond
20 117
55 61
0 23 23
0
0.178 0.143 0.313 0.059
--
0.084 0.141
--
D Resin Process Capabilities
5265
5305
5385
5415
Bulk Density Inherent Viscosity L Color A Color B Color % on Pan
(vs. 2%, max.) % thru 140 Mesh Drytime Mets I.R.
(vs. 95% of control) Hard Particles, (% > 10)
1.28 0.24 3.05 1.78 1.83 4.44
--
0.92
--
--
--
----------- ----
E Compound Oualitv Summary
2.00 0.76 6.89 4.00 2.33 4.89
1.37
--
--
--
--
2.52 0.77 6.17
--
2.00 3.89
--
1.83 0.67
--
--
13.2
0.39 0.67 4.44
--
2.67 4.00 0.67 3.56 1.67 1.62 0.90 1.2
Adjustments
M Lbs. Hi
Hardnes s Color/Clarity Hard Particles Dicing Cross contamination
Total
7.0
-- -- -- --
7.0
(0 Ml)
-- -- --
(0 .11)
Rejections
M Lbs. I%1
----_
24.4 56.8 12.8
2.3 96.3
- - *
(0.37) (0.87) (0.20) (0,Q4) (1.47)
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COMPOUND - continued
F. Drv Blend Quality Summary
Rejections M Lbs. (%)
Long stability
4.2 fO.08^
Total 4.2 (0.08)
Compound SPC Test Results
A n X 3 (i
38401 - Hardness - Specific Gravity - Hard Particles (20")
52 52 52
82.7 1.376
22.3
0.97 0.008 4.4
35031 - Hardness - Specific Gravity - Hard Particles (2')
50 48 51
49.7 1.373 4.9
0.74 0.007 1.9
Mill Temperature Oven Temperature
52 325.5
1.2
All readings 204 degrees C.
5415 Control Resin Test Results
A
n X 3<r~
Moisture
61
0.156
0.024
Drytime
31
5.02
0.51
Particle Size - 60 mesh
56
1.24
0.52
- 80 mesh
62
30.11
6.16
- 100 mesh
62
34.12
1.13
- 120 mesh
62
20.86
2.25
- 140 mesh
62
7.12
0.95
- 200 mesh
62
5.12
1.37
Pan
62
1.10
0.40
Bulk Density
31
0.5051
0.0042
Color - L
31 100.43 0.50
A
31
-0.12
0.37
B
31
2.20
0.61
Flow Time, sec.
31
7.95
0.68
Hard Particles, 7 min.
61
5.31
2.22
Inherent Viscosity
18
1.0122
0.0143
I. Miscellaneous
1. Richard Williams, Billy Sizemore and Dave Cox attended both the rigid and flexible compound training classes at the Best Western on 12/7-8. Harold Coleman attended the rigid class only. Brian Harrison presented his color training presentation as part of the rigid class.
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VAB.0001190665
LABORATORY
I. Miscellaneous - continued
2. Brian Harrison prepared 80273G controls, including +/-20% of master batch, for Premiere Polymers to use on their new dry blend unit.
3. Brian Harrison completed an evaluation of Kemira OR-450 and OR-460 and approved them as substitutes for CR-834/R-101 in all non-weatherable applications. Awaiting PRS results of QUV testing for approval in weatherable applications.
Brian Harrison completed the color match for Lamar's experimental charcoal gray formulations. He also worked on reducing the cost of the orange colorant used in 38401 0RG61 for Corelmex from 7.4 to 0.95 cents per pound.
5. This was "meeting month".
Brian attended the Rigid
Compounds Steering Committee meeting on 12/15. Harold
Coleman attended a CTTC meeting on 12/6, a Resin Business
Team meeting on 12/8 and a 5305 Quality Improvement
(Klockner) meeting on 12/13. Richard Williams gave a Lab
SPC presentation at the Site Coordinators meeting on 12/13.
*
VAB.0001190666
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ruSiDin Ship Date 12/02/88 12/06/88 12/06/88 12/06/88 12/12/88 12/15/88 12/16/88
DECEMBER 1988
Product 5415(OG) 5415(OG) 5415(OG) 5415(OG) 5415 DEBOX Resin 5415
Amount 2X2 lbs.
2 lbs. 2 lbs. 2 lbs. 50 lbs. 2 lbs. 5 lbs.
Customer Hoffman Plastics Tecknor Apex Color Rite Central Syntech Decorative Coverings Osterman & Co. JPS Elastomerics
COMPOUND Ship Date 12/07/88
Product 48562 BLK
Amount 50 lbs.
Customer ACF Industries
DRY BLEND Ship Date 12/19/88
Product 180-31 WHT 138
Amount 1300 lbs.
Customer Astro Plastics
VAB.0001190667